lazylightning@mail.r
Active Member
I went on vacation with my bike this summer. My mother in law and wife were both nice enough to allow me to use their baggage limit so I could bring my bike on a plane for free. They had 10 kg of carry on anyway, so I'm not a tyrant ;-)
While I was on vacation, I was able to spend more time figuring out how to tune my Kheihin 22mm carb that's on my Chinagurl 66cc engine. At one point I was getting mega results, power just became intense and the high end opened up and let me out of the bottlekneck of sputtering at high end that had plaugued me always before. I like to do clutch slips, while barely squeezing the clutch, I rev it out to high rpm's and accelerate fast. Well now I had gotten it to where it accelerated so fast that I got worried about getting used to the new power. The high end got at least 20% faster. Later I was plaugued by unknown problems. Finally I discovered the black wire to my ignition coil was severed, but it was holding on by a piece of insulation. Sometimes I had good spark, then it was bad, and then it was not. So since I had already torn down the engine looking for the problem, I decided to do one mod. I realized that I could widen the intake port at the bottom where it is actually open when the piston skirt comes up. The upper part of the port never being open at all. The small diamond dust file did a pretty good job and I was able to widen it out to under the transfers. The piston ring pins not coming down that far. When I got it all back together, the power boost from the mod was really noticeable. It seemed definitely more responsive at lower RPM's.
I had the bike where it was almost popping wheelies, though I didn't want that. I had to be careful giving it gas too fast on dirt or gravel because it would spin out and drift which posed a danger of laying it down at times. All the locals in vacationland were really pleased with the way it wold take off fast, and I had my new stainless steel gas tank on which had people waving me down all the time. Up in the steep mountain roads, it had more pull than I could use due to the curvy and dangerous roads.
While I was on vacation, I was able to spend more time figuring out how to tune my Kheihin 22mm carb that's on my Chinagurl 66cc engine. At one point I was getting mega results, power just became intense and the high end opened up and let me out of the bottlekneck of sputtering at high end that had plaugued me always before. I like to do clutch slips, while barely squeezing the clutch, I rev it out to high rpm's and accelerate fast. Well now I had gotten it to where it accelerated so fast that I got worried about getting used to the new power. The high end got at least 20% faster. Later I was plaugued by unknown problems. Finally I discovered the black wire to my ignition coil was severed, but it was holding on by a piece of insulation. Sometimes I had good spark, then it was bad, and then it was not. So since I had already torn down the engine looking for the problem, I decided to do one mod. I realized that I could widen the intake port at the bottom where it is actually open when the piston skirt comes up. The upper part of the port never being open at all. The small diamond dust file did a pretty good job and I was able to widen it out to under the transfers. The piston ring pins not coming down that far. When I got it all back together, the power boost from the mod was really noticeable. It seemed definitely more responsive at lower RPM's.
I had the bike where it was almost popping wheelies, though I didn't want that. I had to be careful giving it gas too fast on dirt or gravel because it would spin out and drift which posed a danger of laying it down at times. All the locals in vacationland were really pleased with the way it wold take off fast, and I had my new stainless steel gas tank on which had people waving me down all the time. Up in the steep mountain roads, it had more pull than I could use due to the curvy and dangerous roads.